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First few bits


Kaveney

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No, not me. Live just South of Haywards Heath and she's garaged until the Spring although she has just got back from RTP. Would be good to see you in Brighton and at the South East meets.

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A few more updates over the weekend I got done .

 

Fist up was to clean then condition the leather seats .

 

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Then was the boot counter weight removal .

 

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Then last up was to re adjust the aux and air con belts as there was a little slack and squeaking on start up .

 

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Alan

Edited by Kaveney
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Got a few more bits done over the Easter weekend .

 

Seafoam was done below

 

x 1 can in fuel tank

 

x 3/4 in oil ( run for 100 miles )

 

x 1/4 in brake booster pipe

 

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Then to drain the oil and seafoam out and do a fresh oil and filter change

 

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I changed my rad cap from the OEM 0.9 bar one

 

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To a Mishimoto 1.3 bar one

 

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Then last was changing the induction

 

New Stillen kit with V/S ring

 

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K & N Typhoon Removed

 

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Stillen fitted

 

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Alan

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  • 2 weeks later...

Had a busy long weekend and got a few more bits done .

 

On Friday i went up to Abbey Motorsport for a Milltek Exhaust to be fitted and check the tune on the dyno for the uprev .

 

Old stock system

 

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The back box pipe had been patched up one already .

 

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New Milltek fitted

 

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Then the Dyno sheet that I was not expecting .

 

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+ 9 BHP ad + 7.7 LB/FT from last time and the only changes were the Milltek exhaust and Stillen induction ( last map in Blue HFC , K & N Typhoon , HFC , P/spacer , Uprev )

 

The car started out in November at 225.6 BHP and 217.7 LB/FT

 

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And is now 252.7 BHP and 238.3 LB/FT so that's a + 27.1 BHP and + 20.6 LB/FT gain .

 

Then on to fitting this little lot

 

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First up a grounding / Earth kit that I made up ( X 10 ) and cleaning the original earths .

 

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Then on to the clutch fluid flush / change and S/S clutch pipe .

 

Old clutch fluid not looking so good .

 

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New ATE clutch fluid

 

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Old cutch pipe .

 

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New one

 

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I had some DEI gold heat reflect tape left over so wrapped this around .

 

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And fitted with some protection heat wrap .

 

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Only problem was I had no cutch pressure so had to prime the cutch slave to get the pedal back then bleed the system .

 

Alan

Edited by Kaveney
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Just to note for people looking at the Milltek after 100 odd miles the sound of the system is spot on for me not too loud but gives a nice deep base .

 

This is with Cobra HFC .

 

Also the clutch is so much nicer to use and lighter so I would recommend a fluid and pipe change to anyone .

 

Alan

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  • 3 weeks later...

Another small update as some more parts arrived .

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Earthing kit to add to the smaller kit that is installed .

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Then wrapping the induction pipe in DEI heat tape ( did this on my old Mr2 Turbo and inlet temps came down )

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And to finish off a wax with the G3

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