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The Red Devil


ZaneDylan

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On to prettier things, the carbon hatch I had bought had a lot of scratches and defects, I wet sanded and used several grades of polish to bring the carbon back to life and take out the majority of scratches. I then gave it a healthy coat of Bilt Hamber Double Speed wax. I also took to widening some of the clip holes which allowed me to finally put the interior plastics back in - this reduced a lot of rattle and cabin noise and made everything feel a lot more OE and complete.

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Keeping with the theme of improving the interior, I wanted to tie in the head unit with some more modern touches, I know Ambient lighting isn't to everyone's taste and it can easily be overdone. I removed the door cards, separated the suede part from the rest of the door and laid in my LED strips, then I removed the glovebox and used superglue to stick the glovebox section down as 3M tape wasn't strong enough.

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This is a job I've been putting off... The intake pipe has been covered in gold heat tape - its peeling and it has been applied terribly, is bunched up in many places. I personally don't believe gold tape makes enough of a difference to intake temps to make it even remotely worth it for how bad it looks.

 

So I first struggled with peeling it off and using a heat gun with plastic razors but that genuinely only made it worse.

 

Then I used a chemical sticky stuff remover (goo gone wasn't strong enough)

 

I then gave it a bath in some washing liquid and water before hitting it with a generous amount of metal polish on a drill attachment, I'm happy with the results20.jpg.448d7587c378f18e36c0ae7775effba4.jpg19.jpg.3f55f223f6a99dd0fd9b970af8ea142e.jpg18.jpg.7ebef1c2fbf17e733cc73532c73636c8.jpg17.jpg.384136662ac6a1ddfe098ab15e43ce08.jpg

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Around febuary is when I started to get frustrated with all of the little issues and decided to tackle all of them - first was the intake pipe and polishing in the last two posts. In this post is where I finally attempted to fix my squeaking chair, I removed it from the car, disassembled it and coated everything in spray on silicone. I destroyed the air quality in my house (because UK weather) but I could finally drive my 70 in peace66a1ddab-705c-4360-8c66-12625bd32cd1.jpg.a0cced913b85be50dba45a611b0ab2e9.jpg3a9e64f5-c053-4f41-a67c-4b6c12fbdec2.jpg.77499de2e64577d82a81b0317963e18d.jpga3697eb4-1f0b-453d-9ae1-3d4124a2c938.jpg.2e6e4ba57d2500d9a6220b1cb5d1a0e2.jpg

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Part 3 of the little things, the side skirt extensions 1) aren't to my taste 2) make it harder to jack up the car 3) were battered and loose in places

 

So with a variety of 10, 8 and 7mm self tappers being removed, I took those extensions off and sold them for dirt cheap on market place

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To show off the 2nd coolest mod on the car (boost), I decided to put my genuine Nismo V2 front bumper under the knife. I cut out the grill section and gave my charge cooler a clean and a coat of VHT silver.

 

I used a multitool and a Dremel to perform the surgery and in all honestly its way cooler to see the cooler. I need to cover up those old license plate holes too.a4ef8926-d16c-456b-adc1-92fa890c64ce.jpg.300cc3fa1d7c198296810eb8993b7b7a.jpg1d351732-f02a-4c5e-88cc-f2c6f58639af.jpg.c11cc6ecf4dd65ebc12d4387e8355b75.jpg

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The car from the beginning was giving me an intermittent limp mode issue, it wasn't very often in the beginning, but became more and more frequent, all 4 fault codes it was throwing was pointing towards one thing and unfortunately it is a fault with the stillen supercharger kit. Luckily for me Horsham Developments make a replacement loom for the throttle body and they fixed the issue quickly, as well as my exhaust leaks. I do have the say the new loom not only fixed the issue but also looks a lot nicer, so massive shout out to them.

 

While I was there and now the car was running better than ever we decided to do a dyno run to see if the 530hp I was told when I bought the car was a fib like I thought it was...

 

 

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