ZaneDylan Posted yesterday at 11:36 Author Share Posted yesterday at 11:36 On to prettier things, the carbon hatch I had bought had a lot of scratches and defects, I wet sanded and used several grades of polish to bring the carbon back to life and take out the majority of scratches. I then gave it a healthy coat of Bilt Hamber Double Speed wax. I also took to widening some of the clip holes which allowed me to finally put the interior plastics back in - this reduced a lot of rattle and cabin noise and made everything feel a lot more OE and complete. Quote Link to comment Share on other sites More sharing options...
ZaneDylan Posted yesterday at 11:46 Author Share Posted yesterday at 11:46 Keeping with the theme of improving the interior, I wanted to tie in the head unit with some more modern touches, I know Ambient lighting isn't to everyone's taste and it can easily be overdone. I removed the door cards, separated the suede part from the rest of the door and laid in my LED strips, then I removed the glovebox and used superglue to stick the glovebox section down as 3M tape wasn't strong enough. Quote Link to comment Share on other sites More sharing options...
ZaneDylan Posted yesterday at 11:56 Author Share Posted yesterday at 11:56 This is a job I've been putting off... The intake pipe has been covered in gold heat tape - its peeling and it has been applied terribly, is bunched up in many places. I personally don't believe gold tape makes enough of a difference to intake temps to make it even remotely worth it for how bad it looks. So I first struggled with peeling it off and using a heat gun with plastic razors but that genuinely only made it worse. Then I used a chemical sticky stuff remover (goo gone wasn't strong enough) I then gave it a bath in some washing liquid and water before hitting it with a generous amount of metal polish on a drill attachment, I'm happy with the results Quote Link to comment Share on other sites More sharing options...
ZaneDylan Posted yesterday at 11:57 Author Share Posted yesterday at 11:57 As shown in the last update the timing chain cover is also pretty dull, so I gave it two passes with alubright and tried to polish everything I could reach Quote Link to comment Share on other sites More sharing options...
ZaneDylan Posted yesterday at 12:04 Author Share Posted yesterday at 12:04 Around febuary is when I started to get frustrated with all of the little issues and decided to tackle all of them - first was the intake pipe and polishing in the last two posts. In this post is where I finally attempted to fix my squeaking chair, I removed it from the car, disassembled it and coated everything in spray on silicone. I destroyed the air quality in my house (because UK weather) but I could finally drive my 70 in peace Quote Link to comment Share on other sites More sharing options...
ZaneDylan Posted yesterday at 12:08 Author Share Posted yesterday at 12:08 Part 3 of the little things, the side skirt extensions 1) aren't to my taste 2) make it harder to jack up the car 3) were battered and loose in places So with a variety of 10, 8 and 7mm self tappers being removed, I took those extensions off and sold them for dirt cheap on market place Quote Link to comment Share on other sites More sharing options...
ZaneDylan Posted yesterday at 12:14 Author Share Posted yesterday at 12:14 To show off the 2nd coolest mod on the car (boost), I decided to put my genuine Nismo V2 front bumper under the knife. I cut out the grill section and gave my charge cooler a clean and a coat of VHT silver. I used a multitool and a Dremel to perform the surgery and in all honestly its way cooler to see the cooler. I need to cover up those old license plate holes too. Quote Link to comment Share on other sites More sharing options...
ZaneDylan Posted yesterday at 12:20 Author Share Posted yesterday at 12:20 (edited) I swapped out my spark plugs for some GTR plugs (one step colder) then went off the PetrolHeadism and took plenty of pictures that weekend, had a great time with great people Edited yesterday at 12:21 by ZaneDylan Quote Link to comment Share on other sites More sharing options...
ZaneDylan Posted yesterday at 12:27 Author Share Posted yesterday at 12:27 The car from the beginning was giving me an intermittent limp mode issue, it wasn't very often in the beginning, but became more and more frequent, all 4 fault codes it was throwing was pointing towards one thing and unfortunately it is a fault with the stillen supercharger kit. Luckily for me Horsham Developments make a replacement loom for the throttle body and they fixed the issue quickly, as well as my exhaust leaks. I do have the say the new loom not only fixed the issue but also looks a lot nicer, so massive shout out to them. While I was there and now the car was running better than ever we decided to do a dyno run to see if the 530hp I was told when I bought the car was a fib like I thought it was... Quote Link to comment Share on other sites More sharing options...
ShortPaul Posted yesterday at 17:06 Share Posted yesterday at 17:06 Great work mate,the car is looking much better now 😁 Quote Link to comment Share on other sites More sharing options...
Recommended Posts
Join the conversation
You can post now and register later. If you have an account, sign in now to post with your account.